Worn Spindle Interim Solution

From: TheMole (dbilesky(at)cln.etc.bc.ca)
Date: Sun Jul 27 1997 - 19:26:34 CDT


Yesterday my insurance was due along with the local 'Air Care' test.

Without time to order and receive new Throttle spindles as I found my car
uses the carbs from a GT6 I improvised.

Using vacuum line plugs that matched to spindle diameter I cut them short
and punched holes in the ends.

This I used to cap either side of each Stromberg where the throttle spindle
comes out.

I leaned out to the max + 1 and had the car tested.

FAIL

The failed component of the test was Hydrocarbons at idle. I went past the
max allowable and past where the meter stops reading. An indication of
fresh gas blowing out the tail pipe.

As this seemed like normal operating conditions I was stumped.

I replaced the spark plugs and they all looked fine.

I replaced some hoses too.

I tightened the linkage and welded the bracket on the firewall the gas
peddle links to when it enters the engine compartment. This has always
been very loose.

I put some new filter material in the carbs.

The filter inserts used for shop wet vacs is very close to the right
diameter.

After syncronizing again, extra super lean + 2 and a tank of Super Octane
92 I went for a test.

FAIL

The lean nature of the carbs forced the car to run poorly and the choke
solution smoothened out the
ride.

However, something else was up. I pulled each plug wire off as the car was
running and found #4 to not have much of an effect, although there was
plenty of spark.

Compression test gave a reading of about 20 where 2 and 3 were 165 and 1
was 135.

I removed the valve cover and found the rod tightly jammed up against the
rocker. I regapped. Looks like a situation where the valve is either
being stretched or the head is collapsing thus never allowing the valve to
close. Fresh gas blow-through zone.

There was still enough room dispite the lengthening valve to allow the
valve to close.

Looks like a head rebuild coming up

Replaced all removed parts. Re-tuned to 'it is not so lean nothing should
get through + 3'

and re-tested.

Is was 5 pm on Saturday, I was the last car.

Maximum allowable reading 1500, My car 1420.

PASS

Oh, I put a PCV between the bottom engine vent and the intake manifold.
When I replaced a few hoses I put it in backwards and ...

Oil leaked out of that car from everywhere.

..

Just thought I would pass on my adventure.
Next year I go through this whole thing again.

dgb



This archive was generated by hypermail 2b30 : Tue Sep 05 2000 - 09:48:07 CDT